I have a very annoy problem after a defective 8 bit alexmos gimbal controller i bought a new one but as u see whatever i do i can make it work please see the video and help i am desperate
I would say the gimbal is working just as can be expected, when holding the IMU in hand. It needs to be well fixed to the camera an right position and the orientation configured correctly on the GUI.
HI. I am having the same problem with the IMU mounted to the camera. Simply spazzes out even after numerous 6 point calibrations. Any guidance or thoughts would be great.
Just do the one point calibration and only once. that is enough to get it operating correctly. 6 point calibration will just improve the performance if performed right. You can do the 6 point calibration after everything is first working.
Have you followed carefully all the steps in user manual, assigning motors correctly, setting the inverted status correctly, telling the GUI how the IMU is installed etc. remember press write after changing the values.
It is also possible that it was not only the board that was defective. The motors or IMU could be defective too, or wires.
Do you get I2C errors, what does the real time display show.