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Nebula 4000 (8Bit fw 2.40b6): pitch strange behaviour
  • Hi all, first post here. After trying to tune PID settings the gimbal, the pitch isn't working anymore, even after uploading the factory settings.
    Anyone has an idea of what it could be?
    When almost levelled the axis is compensating, but after few degrees (5-7) tilting backwards or forward it start bumping more frequently the more the tilting angle is.

    http://youtu.be/GOYlvk0nkD4

    Thanks in advance