So my prob: the yaw and pitch motors are missing steps, like literraly (not only erro in gui) - i can see it on my gimbal. I even set max 255 power with high sensitive mode for picth but if you rotate the frame a little bit - the picth motors try to stay horizontal - but it can't reach the horizontal state: exactly like in that discussion: http://forum.basecamelectronics.com/index.php?p=/discussion/1120/strange-behavior-of-roll-axis#Item_1.
What i've tried: 1) i switched pitch motor to roll out - and it works like a charm.if i connect it back to pitch out - it behaves like above 2) i checked all motors - all resistance are fine 3) i checked motor drivers on the board - the pins that leads to motor pins are fine 4) tried different pids 5) calibrated gyro and 1 point accel 6) tha bord looks fine
For me it seems that yaw and pitch outs behave like the motors would if they are missing phase - not enough torque. All looks fine, but doesn't work. Any thoughts?
P/S i can't reset controller. I tried to set reset controller in service for the button - but looks like nothing happens after it's pressed. I tried to press/hold button on the board - still nothing. Is there any software way to reset to defaults?