I get response in realtime graph but my yaw motor does nothing
  • I have a 3 axis 8bit Alexmos board. Rig is balanced on all axis. The pitch and roll I can tune but the yaw no matter what I set it at does not move. All connections look good and did work in the past. Any suggestions? How can i narrow down to if a motor problem or an electrical problem? Any help will be greatly appreciated and will help stop me from pulling out the rest of my hair.
  • Hello,
    Please, make screenshots of Basic and Advanced tabs of the GUI and place here.